Thats what they sell masking tape and sharpies for.
Looking good.
Bill
Printable View
Thats what they sell masking tape and sharpies for.
Looking good.
Bill
Yup.......Been there done that trip.......
Butttttttttttttttt.....Most electrical connectors are item/location specific and will only go one place.
It lives!
Started it for the first time this morning. Checked for leaks after the first two non-firing cranking sessions. Found a pretty significant fuel leak on the forward end of the right fuel rail. Seems I forgot to tighten the fuel line nut (pointed to in photo below) that feeds the rail... :eek: Only needed to remove the alternator and AC compressor (to get the alt off). Luckily, I could get my 3/4" claw-foot and an extension to work with my tq wrench to reach under the wiring bundle in that area. That fitting is tq'ed to 30 ft-lbs. I think it's leak free now.
https://www.thedieselpage.com/images.../rail-leak.jpg
No abnormal pressure buildup in the cooling system, which is why all this was done in the first place. Starts and runs really well. Drove it a few miles to burp the cooling system. No SES lamp or trouble codes. Sounds a little different than before.
When re-installing all of the coolant-related parts on top of the engine, I noticed that most of the gaskets and o-rings had been leaking/oozing a little over time. I suspect that the cooling system over-pressure the engine had been having over a long time worked on the gaskets/o-rings too. I replaced all of those gaskets/seals/o-rings and installed new thermostats. The rubber gaskets on the t-stats had been leaking a little too, and they weren't properly regulating engine temperature - ran a little on the cool side.
Once the engine cools overnight, I'll change the engine oil and filter, then re-install the wheelhouse liners. Hopefully that's it. "Only" about 80 actual hours start to finish, not counting the ~400 mile round trip to get the heads resurfaced. No broken parts, no lost (or "left over") bolts/hardware, no broken electrical connectors, no scratches on the truck, just a few scraped knuckles, got a better result for far less money... New SAC00 injectors, new updated "C" grade head gaskets, new injector hard lines and ARP studs, plus some new tools (including two small torque wrenches) for something over $4K. I'll have a more accurate accounting when I go through the pile of receipts. This job would have cost $10k if you'd hired it done...
Thanks Bill,
Mostly kidding about the electrical connector puzzle...
Although, it took me a while to figure out one connector on the driver's side. The answer came when I remembered that it was for the oil pressure sender connection to the engine harness. On the passenger side, I had this important-looking connector on the harness that had no mate on the engine, then I remembered it was for the MAF sensor on the airbox (which was sitting on the parts table). And lastly, the glow plug controller module has 4 connections. I didn't do a good job documenting the wiring, so I had to dig through my photo archive to find a photo of a wired GPCM. The best photo I had only showed a part of the module, but after some head scratching it was enough. Every other electrical connector was, as Robyn said, pretty much self evident - there are so many of them...
Good to hear that things went reasonably well....
The first start up after a major tear down is always tedious and usually bends the nerves a bit.
Looking forward to hearing the results of the road test.....
Congratulations Jim!
Glad to see you got it up and running again. 80 hours isn't so bad for a guy who doesn't do it for a living....
Way to go!
Dave
Deja Vu - photo taken just 10 minutes ago... It begins again...
https://www.thedieselpage.com/images...asket/Deja.jpg
Take 2?
There was once an "incident" with nitrous... producing a nagging cooling system overpressure. I suspect a couple of the head bolts may have yielded a bit. The first head will come off later today or tomorrow, depending on how much time I get to work on it. Working on the engine is generally easier in Lil Red than it was in the GMC - the truck is lower, and there's more room in certain areas (rear of the driver's side head). Plus Lil Red has a lot fewer miles (about 10k), has never been apart before and has never seen road de-icer.
Sounds good.....
Be interesting to see what actually happened...and why the pressure issue....
Robyn,
My thoughts about the causes of over-pressure problems are evolving. My thinking at the present time include:
1- The head gaskets simply wear out over years of use due to the friction caused by differences in the coefficient of expansion rates between aluminum and cast-iron. I suspect there's a direct correlation between thermal cycles and head gasket life (in the case of my GMC - 15+ years and 140,000 miles), at least with the original crimped head gaskets.
2- Head bolt(s) yield for whatever reason (especially when beyond stock power/boost levels), which reduces the clamping load - resulting in combustion pressure leaks. With Lil Red, there's a direct connection in time between a nitrous backfire at the track and the first appearance of the cooling system overpressure... What's interesting is that GM reduced the head bolt torque angle settings (reduced the torque) of the same TTY head bolts when installing the newest riveted head gaskets. Perhaps the earlier/original crimped tabs were interfering with head bolt clamping force.
3- The original head gaskets used crimped tabs at various places around the perimeter of each gasket. These crimped tabs were what kept the multi-layer gaskets locked together. The tabs are thicker than the surrounding gasket and are located between the head/block surfaces - making it harder for the head bolts to effectively clamp/seal the gasket. You can see what effect this has on the gasket and where most of the questionable sealing occurs. The new riveted design has the riveted areas outside the head/block mating surfaces, so they don't interfere with the effectiveness of the head bolts to maintain clamping load over time.
I watched an ARP video a while back where they discussed the "elastic" clamping load supplied by properly installed and torqued Series-2000 head studs produced for the Duramax. I like it that the ~$650 head studs have some elasticity designed-in.
However, we know that GM is still using TTY bolts in the newest L5P Duramax, which is rated for 445 hp / 910 lb-ft - and rated for up to a 35,000-lb GCVWR.
I interviewed the "Duramax Power Tour" team in 2000, who drove an LB7 equipped 3500-series truck towing a 20,000-lb event trailer. I rode in that truck as they wailed on it, on the I-90 continental divide pass just east of Butte, Montana. I asked them if they drove it like that all the time. I was told yes... They put in excess of 20,000 miles on that truck - hammer down all the time. I can also point to a 750,000-mile LLY Duramax used to commercial tow RV trailers all over North America, that I wrote about a few years ago. GM could acquire head studs equal to those offered by ARP (maybe even contract with them to provide) if they felt it was necessary.
I have a couple of debate points about studs that are hard to answer and difficult to challenge. 1- The aftermarket pushes anything that they can sell - ("while you're in there") type of stuff, including head studs. 2- Studs are simply easier to install than TTY bolts. You must mark the heads of each TTY bolt during the two angle tightening sequences or you'll mess up the installation. With studs, you only use a torque wrench. If you forget one or get out of sequence, it's really easy to check what the torque is for that stud. Personally, I think this is why many vendors/mechanics push studs (sell more expensive stuff and they are easier to install). Otherwise, they would/could point to actual durability tests involving direct comparisons between engines using head studs and TTY bolts (fleets would be the best source of information. Second best would be an accumulation of real-world reports from actual owners - like the story I did on the 751k mile LLY Duramax). For most, these head gaskets will wear out long before any real comparison can be done on the veracity of claims otherwise.
I plan to measure the actual torque applied to these TTY bolts after completing the 2-step torque angle installation. We know that GM/DMAX reduced the final TTY head bolt torque angle setting when they introduced the new updated head gasket in 2007. I suspect this was to reduce the Brinelling of the head gasket fire-ring onto the aluminum heads. Knowing what the torque is for current ARP studs (125 ft-lbs), it'll be interesting to learn what the actual torque value is for the installed TTY bolts. The current TTY installation takes the TTY bolts from a static torque installation setting of 59 ft-lbs then adds two separate 60 degree rotations for a total 120 degrees. The original Duramax TTY bolts saw a 150 degree sweep after the 59 lb-ft static tq setting.
I agree 100% on the TTY BOLTS.....A cheap easy fix instead of doing it the right way..
You drive the rig with great care and NOT ...HAMMER DOWN .....The stock stuff will work.....
Take it into the ozones a couple times.....Maybe it will survive....maybe not......
A bolt that is already into it's elastic mode and then hit hard......all bets are off.
TTY BOLTS are more like taffy.......
A bolt that can stretch a little and come back will be far better than one that is into the"GOOOY PHASE" and then the extra hit simply stretches the bolts out waaaaay too far......."The bolts you found with less breakaway tension.
I have found the same mentality with the big snow cat.....do it cheap and dirty.....Yeah...good for a while...but when it fails ...things get ugly..quick.....
Are you going with studs on "Li'l Red" ?????
A six and a half with REASONABLE power levels will do fine with TTY bolts.
Try shoving big boost and a buttload of fuel into a 6-1/2 and it will suffer....
I tried a set of MLS gaskets on a 6.5.....NOT ENOUGH HEAD BOLTS IF USING TTY..
ARP studs may have worked better.......
The factory stuff is always right on the ragged edge.....You always need more when you plan on flogging it hard.....
If money is no object, we would all live life differently and make different decisions regarding diesel engine service. Fact is, the ARP head studs are $650 and the factory TTY bolts are about $100.
Take an old truck to a diesel shop or dealership, and ask them to install a new head gasket kit ($400), ARP head studs ($650), new injectors ($2400), new injector hard lines ($650), new water pump ($125), new hoses and an endless list of "as long as we're in there" stuff, and of course at least $5k in labor - and you've made a bad decision regarding financial common sense - i.e. spending $10k+ on a truck that in even perfect condition is still only worth 10K. When faced with that reality, most thinkers will crush/part-out the truck and not spend a dime on it... We didn't even talk about brakes, ball joints, steering components, drivelines, tires, rust... and on and on and on...
Meanwhile, our performance 6.5TD Project ran without a problem to 300,000 miles in 7 years using TTY head bolts (till we sold it), and my 2001 GMC ran to 140,000 miles using TTY head bolts - even with the poorly designed factory crimped-style head gaskets. I get where the ARP stud advocates are coming from. This is partly why I installed ARP studs in my own 2001 GMC LB7 head gasket repair. I spent extra on this truck only because I did the work (and because I needed to install the studs so I could photograph it and eventually write about it). It's just that at some point, all those faced with a significant repair on an older truck need to make a decision... Do you crush the truck or do what is necessary to save it without compromising basic service and dependability while not violating financial common sense? As part of an overall budget strategy, I think the lower cost TTY head bolts fit into that paradigm. And... Lil Red is getting TTY bolts.
What would mean most to me regarding this studs/bolts debate is to study the actual service histories comparing engines built with studs/bolts along with a description of how the trucks were used, and then be able to discern some sort of recommendation from that. Right now, the stud advocates "say" they are better... We can read about tensile strength and a wide range of engineering theory, but what's that really mean in the real world to average truck owners?
Pretty much spot on..
Trying to do a "Budget" rebuild any more is a real challenge.
I am trying to build a 406 Small block Chevy for the snow cat....
Used Vortec heads in great shape (Zero cash outlay....Sold the short block to recover the total cost)
400 block $150 plus $350 for machine work
Pistons....New ebay score for $135
Good used stock crank.....$125
Still need the cam/lifters
Timing gear/chain
Gaskets
Oil pump
Fuel pump
Push rods
Have new high capacity pan $175
Flex plate
And on it goes.
Have a fresh carburetor $127
New exhaust manifolds $175 pair
Intake manifold for Vortec heads to fit 4 barrel carb.....$100 plus
No matter what it is....even when you do all the wrenching yourself.....$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$ $$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$$
Adds up quick
"new injectors ($2400)" Are you writing about a 6.5 GM diesel? That's $300 per new injector?
That price is for remanufactured Duramax LB7 injectors. "New" as in replacing what was originally there. Prices vary between vendors. You can buy suspect stuff off eBay for less or spend a lot more for newly manufactured Bosch injectors. The $2400 price is for reman from Kennedy. Injector prices for newer model Duramax engines are more.
I had hoped back more than 15 years ago that injector prices would fall for the older model Duramax. I knew that as the truck's book value dropped, a critical point would eventually be reached where the cost to repair exceeded the "drop dead" percentage of 50% of vehicle value.
There is light though... I'll need to spend some time investigating, but it is possible to do what was unthinkable just a few years ago and replace the wear items in these injectors using only basic tools and skills. This, I believe, will become a big factor in saving the older trucks.
With a basic "Pop" tester you can check the pop pressure and observe the spray pattern.
Not quite as good as the tooling the big boys have....but you can get the job done.
Replace the nozzles and a few other small parts.... then shim the springs to get the pop pressure right.
I have done a few sets of "Squirts" for the 6.2/6.5 and other than the time to fool with them....They were fine......
I can't imagine the units for the DMAX being any tougher to do...
The LB7 squirts from what I have read were basically flawed from the get go and tend to be very fussy about any dirt in the fuel......
Be fun to rip into a set and give it a go.....
In theory.
But, it isn't that simple. I'm not too optimistic. Parts can be replaced, but that's about where it ends for the consumer. Capable test equipment would be necessary, as well as tools and a clean environment. The parts are relatively inexpensive and available, and not too difficult to replace, which creates a difficulty (at least for me) in seeing where the replacement cost of reman's comes from. I suspect they charge what they do, simply because they can. Bosch factory new and remans are costly, and non-Bosch rebuilders base their pricing on the Bosch list price. The actual cost of rebuilding these things is MUCH less than what they sell for. The profit margin is ridiculous, at more than 300%. I've researched it, and that's the most generous figure I can come up with. The parts, tools, labor and time just do not add up. For the cost of 2 or 3 retail injector sets, a shop can fully equip a station capable of quality full rebuilds, and a full set can be rebuilt and tested in a couple hours or less. Of course, it isn't that simple, but it certainly is not 300-500% more complicated. The same argument can be made of 6.2 and 6.5 injector pumps.
The LB7 injectors can see up to 23K PSI (later models are significantly higher), and idle at 4K+, and are fired by a solenoid, and will fire multiple times for each injection event (pilot injection, up to about 2700 RPM's). The volume of fuel is similar to the 6.5, but at the LB7 pressures, as with any hydraulic system, pressure and volume can be traded. Increased pressure decreases necessary component volume for the same fluid volume. Contamination becomes much more critical as the component parts become smaller. Herein lies the problem. The internal fuel volume components of the Duramax injectors must be very small, and meter fuel precisely. Known material failures aside (there have been a couple), that high pressure working against the tiny components results in erosion over time, which is also more rapid with greater fluid contamination. SAC nozzle injectors address much of the durability issue, but at a cost of less precision. Everything is a trade.
That's the crux of what I'm talking about.
There are a lot of really good vendors out there - who have done a lot to push forward the service and performance of these diesels. But... it is a business, and some, unfortunately, are losing sight of the big picture. Unaware of what is happening, they are driving out both the older trucks and those new (read young) diesel owners who are the future of the market.
I've watched a lot of youtube videos recently about a range of Duramax repairs. Most of the videos are produced by 20-somethings to 30-somethings, some even doing the work (big jobs) in a car port... some in northern winter weather. Many are doing it because they can't afford a newer truck or can't afford to hire the work done. Everyone should realize that these are the new truck buyers a decade from now... unless the cost of repair parts drives them running and screaming away from diesels in general and the Duramax in particular. Generally, it's the kids who are buying many of the 10-20 year old trucks. GM has a stake in all this (creation of owner loyalty)... So does the aftermarket.
Something new! I pulled all 8 of the injector cups from the heads in Lil Red. Seven of the cup seating areas inside the heads looked pretty much identical to the following image.
https://www.thedieselpage.com/images...n-Track-02.jpg
I noticed while pulling the injector cups from this set of heads that they pulled quite a bit easier than they did from the heads in my GMC. It appears that there was very little sealant used on the cup tips when installed at the factory.
The following cup seat image shows what looks like carbon tracks due to a combustion pressure leak. The stainless steel cup had matching identical discoloration on it as well. Sorry for the slightly out of focus image. It's hard to get the camera to focus that deep into the head. I should have used a pre-set focal distance setting on my DSLR with an F11 or smaller aperture, but I didn't want to fiddle with it (end of a long day). So, I used my iPhone. This is the #8 cylinder, where the slightly loosened head bolts were found. Possibly the result of the nitrous...
https://www.thedieselpage.com/images...rbon-Track.jpg
That's an absolute indication of....something. Likely, at least, a contributor to your pressurized coolant. What's the origin of the engine? I'm sure we discussed it before, but I don't recall.
I agree on the small parts, high pressure and erosion..
At the pressures used in these systems it takes little abrasive to go to work on the metal.
When you consider the amount of time these parts are subjected to the abuse they take.....no wonder at all that they wear out.
Old school squirts like the 6.2/6.5 are pretty basic.....add the electronics to the mix and the issues get far more complicated.....A simple pop tester will not operate the Dmax injector.....
Working in a clean environment is an absolute.....
Follow factory protocols for the rebuild....No different than anything else we do when building an engine.
Can it be done at home in the garage.....yup.....I would not hesitate to go at it....just need specs on stuff is all.
I rebuilt several sets of Squirts for various 6.2/6.5
Are the ones done by many so called experts any better. ??????? Depends on the tech doing the job....Does he care about quality and is as finicky as we would be.....Big IF right there...
As far as pricing goes...
Here is an analogy of WHY THE COST.
I priced out new track belts for my cat project.
Go to snow cat supply company....1 belt 8" wide and 287-1/2" long $595 per belt
Go the the people who make the belting and spec it out $180 per belt for the same part..
BECAUSE THEY CAN CHARGE UP THE WAZOO.....and they will do so......
When I was in the fabrication business if I ordered a bearing for an overhead crane wheel or drive it was around $75.00. But if I went to my local bearing house and matched number $8.00. A lot has to do with it fitting by application. Another comp is front wheel bearing for a 66 Chevy Biscayne and a 66 Cadillac. Same part number but different price.
Yeah buddy.
When I did the cat differential last summer/fall all the bearings had to be replaced (Water damaged)
Luckily the numbers were still readable.
The inner pinion bearing is a big roller bearing. And at $700 and change for the bad boy...../I went shopping.
Found a new one on ebay.....Located in New York state......$20 including shipping....
All the bearings came off ebay......all top brand names and exact part numbers..... averaged about $20 each.
16 big bearings in that sucker.....
If I had gone to the snow cat parts supplier.....I would have needed to mortgage the ranch...
Yes....prices are much variable......
Here's what it looked like when I received it from GM... after it was uncrated. The Allison it came with had been used in a test vehicle. The engine looked assembly line new, but I thought it odd that the glow controller hot lead had been clipped off. I received this engine in the spring of 2002. I had assumed this was a new assembly line engine - a 2002 model year, but it was actually a 2001 model year CA emissions engine. The glow controller and glow wiring is the main difference between a CA engine and a 48-state Federal emissions engine.
https://www.thedieselpage.com/images...nal-Engine.jpg
It was at this point that I wish I'd clear-coated all of the aluminum components on the engine. So bright and shiny!
I've always doweled several bolt holes and slowly lowered the head onto the block. Never gave it more thought past that. Is there something not obvious about the job, other than preventing a mishap that could damage the head? Your method looks very effective, though.
Not sure exactly what you mean by "doweled several bolt holes".
I watched a guy on youtube set a Duramax head onto a block (that was on an engine stand) after having already set all of the ARP studs in the block. Maybe he was a clod, but he had to get help after having floated the head over (and making contact with) all 18 studs and still not getting it on. I'd bet that head was scratched all over the deck. Even if done perfectly, I don't think that's possible in-frame with the cab on - certainly not on the driver's side. I know that the rear corner of the driver's side head bolt/stud must be inserted into the head before being lowered into place because of interference with the firewall.
My main motivation was about not damaging the head decks and gaskets. Cast iron heads are easier to deal with in this regard.
"Doweled" as in, wooden dowels in the holes. I've used old head bolts with the heads cut off, as well (removed with a vice-grip). If clearance was an issue, short dowels. Wooden dowels got a screw in the end so they can be fished out with a magnet. If I had to use head bolts (never had to), I'd slot the ends so they can be turned with a screwdriver, then fished out with a magnet. I learned this from a retired Ford technician (50+ years) neighbor when I was a teen. He said he had a set for every engine and vehicle he worked on, and never just "tossed" a head on a block. "It's just too easy to do it right the first time." All of my first vehicles were basket cases (dirt cheap or free), so I got a lot of experience. I paid more on DMV fees and insurance than vehicles for many years.
I have both heads on, and the first two initial bolt torque settings applied. Next step is to complete the TTY torque angle settings (2 passes at 60 degrees each).
https://www.thedieselpage.com/images...early-done.jpg
This is how it looked late yesterday. Nearly done! Maybe I'll attempt a restart later today.
Now I know why some mechanics like ARP studs... They are a lot easier to install. Took me about 2 hours to take all 36 bolts through 2 sequences, what with the setup for each torque angle setting, and wanting to do the best job I could... while in the truck. I watched the TTY head bolts installed at the DMAX plant in Morraine, Ohio back in 2001 - they are all installed at the same time by a machine... Took maybe 30 seconds for each bank. I was thinking of that day while fiddling with the angle card setup for each bolt.
Completed the 1,254th step (somewhat hyperbolic) in the process late yesterday afternoon. I had spent some time priming the fuel system using the hand pumping plunger on the fuel filter housing while using both the bleeder screw and the fuel test Schrader port. The engine started on the second 15 second cranking cycle. Purrs like a kitten. There were no check engine light or leaks. I was extra careful to make sure every potential leak source was properly installed and tightened before moving on to the next step.
I shut it off, and spent some time looking everything over, then re-started the engine. Now, there was a service engine soon (SES) lamp. I shut it off, and looked under the hood for anything out of place. I found that the MAF electrical connector had become mostly unplugged. I straightened that out, which must have been due to not getting it latched completely, and the fact that I had to push and pull the air duct to get the new AFE air filter installed - all of which moved the MAF sensor around. However, getting the MAF re-plugged didn't turn off the SES. My Predator programmer won't communicate with this truck... it's married to my 2001 GMC, so I don't have a code to report. Does anyone know if a MAF code has to be cleared or does it go out on its own? Of course, I don't know for sure that the SES is due to a MAF code...
However, the truck runs great! I drove it about 15 miles to warm it up and to burp the cooling system. Makes so much power! It purrs... And, no excessive pressure in the cooling system. Yay!
Your Predator should at least be able to read and clear codes on any LB7, even if married to another VIN. It won't allow any programming, but should read codes fine. I have an early model married to my 2001, and it will read all LB7 and some 04-05 LLY trucks (2006 LLY was a transition), as well as a bunch of other non- CanBus brands and models I've tried. If it doesn't read, check that the OBD port has 12V power, which is required. If it doesn't have power, the tool will seem to power up, but won't do anything (communication error), like plugging it in with the key off, on a truck that's known to work.
The MAF codes are immediate, meaning the PCM only acts if the code condition is presently active. Otherwise, it will remain in history for several start and warming cycles, with the SES lamp on. After the SES turns off, it will remain in history for 40 cycles, IIRC. If you have an active MAF code, you should notice the engine running different. It resorts to a default fueling map, which is very conservative. Unplug the MAF and give it a test. If you don't notice a difference, then it's still faulting that series of codes.
The Predator powers up, and says" Establishing Communications..." or some such, but stays there for as long as I have patience for (with the key in the "RUN" position).
There is unswitched 12v power on pin 16 and a solid ground on pin 4.
https://pinoutguide.com/CarElectroni...i_pinout.shtml
By the way, this lack of communications was present before the tear-down. I wanted to record the injector fuel rates before beginning, but couldn't. And, this truck is running a Kennedy ECM, if that makes any difference...
Update Friday morning: I started the truck last evening, and saw that the SES lamp was gone. Apparently, the prescribed number of ign/start/warmup/cycles allowed the SES to go out. Still a puzzle why Lil Red's test port doesn't allow connection to the ECM. The wiring harnesses were all new factory items when the truck was first put together...
I suspect the ECM plays at least a part in it. I've used 3 Predator tools on several trucks, and some of them had Hypertech programming or plug-in modules in them, and it was able to read/clear codes, as well as read real-time data. I mention the 12V power at the connector because some of them had the power missing at key-off, but worked once keyed on. There were probably other issues at play that I don't recall, but it's happened more than once. It may have been due to a power module or some harness hacking. If yours powers the tool before keying on, it isn't the issue. You possibly could have used the PCM from the 2001 in Lil Red to read the engine data. It may still have some use for benchmark data, and for a comparison between the two, if it works. I don't know if it will, and I've never tried it.